Analysis of Electrical Submersible Pump With 120% Overload Setting Point in the SLN Area

Journal Title: International Journal of Current Science Research and Review - Year 2023, Vol 6, Issue 12

Abstract

In the SLN field, there has been an increase in the setting point by 120% to optimize fluid production and minimize the production decline previously caused by a setting point of 110%, which resulted in temporary well shutdowns. Wells HFU01 and HFU02 in this area experienced shutdowns, suspected to be caused by overload in the electrical submersible pump. Overloaded pumps were identified through alarms originating from the switchboard on the surface, where the alarms were triggered by three cables connecting the switchboard to the motor of the electrical submersible pump. This study aims to determine the impact of overload setting point on wells HFU01 and HFU02, which have not shown improvement after the overload setting point adjustment. The research methodology involves analyzing pump failures due to overload in the electrical submersible pump in wells HFU01 and HFU02 located in the Sumatera Light North Area, which affects the well production. From this research, it is suspected that the wells that have not shown improvement after the overload setting point change may be caused by worn-out, aged pumps with low efficiency, and pump cavitation issues. Through this research, these issues can be addressed, leading to improved well production and run life of the electrical submersible pump, ultimately reducing pump failures in the wells.

Authors and Affiliations

Ghanima Yasmaniar, Hayafa Fakhriyatul Ummah, Puri Wijayanti, Apriandi Rizkina Rangga Wastu, Ridha Husla, Havidh Pramadika,

Keywords

Related Articles

Determining The Contract Service Strategy at Coal Terminal Maintenance to Address Contractor’s Inability to Maintain Availability of Fixed Plants in Supporting Shipments Activities at PTKPC a Case Study PTKPC, East Kutai, East Kalimantan, Indonesia

PTKPC, a coal producer, was facing challenges due to a permit transition in December 2021 from Coal Mining Contract of Work (PKP2B) to Special Mining Business License (IUPK). This change increases operational costs with...

The Influence of Service Quality and Price on KRL Commuter Line Route Solo - Jogja to Customer Loyalty

Transportation as an important element in human life, plays a role in facilitating daily activities and supporting the economy. But because of the heavy traffic caused by so many motorized vehicles, people are looking fo...

Financial Analysis for Land Reinforcement Project to Optimize Dump Capacity INL Pit Case: Coal Mining Company PT. XYZ East Kalimantan

PT XYZ, a leading coal mining company in Indonesia located in East Kalimantan, boasts a production capacity of 55 million tonnes annually. Engaging in coal mining and sales for domestic and international clients across d...

The Influence of Teamwork and Work Environment on Service Quality through Job Satisfaction

Optimal service for public service users is a necessity for increasing citizen satisfaction. The determinant of service quality lies in employee performance. There are several factors that influence service quality, incl...

Applying Scrum Methodology into the Production Processes of a Logistic Equipment Producer

The manufacturing is a competitive domain with a lot of challenges. Products need to be fabricated quickly, cost efficient and always responding to the changing demands of the market. Lifecycle of the products is decreas...

Download PDF file
  • EP ID EP725022
  • DOI 10.47191/ijcsrr/V6-i12-33
  • Views 20
  • Downloads 0

How To Cite

Ghanima Yasmaniar, Hayafa Fakhriyatul Ummah, Puri Wijayanti, Apriandi Rizkina Rangga Wastu, Ridha Husla, Havidh Pramadika, (2023). Analysis of Electrical Submersible Pump With 120% Overload Setting Point in the SLN Area. International Journal of Current Science Research and Review, 6(12), -. https://europub.co.uk/articles/-A-725022